Hi and happy new year to anyone still following this lot. Things slowed down over December, January got shot to hell with work, and now it's Feb... But here's another chance to restart.
Since I last posted, I had a couple of things sorted out:
- the crank was reground straight according to bearing measurements. So now all of the clearances are where I want them to be.
- The flywheel was refaced, and I just opted to get a new clutch kit as I wasn't happy with the pressure plate. Nothing fancy... Just a LUK generic which will serve well enough for now
- Soda blasted, cleaned and rebuilt the carb for the run in period
- Cleaned up the inlet manifolds for later
- Cleaned up my dad's old hobby lathe which has sat around for 30odd years. It's running now, but needs a little more work to true up the chuck and get some cheap cutting tools to learn with
So, on to my next steps. I want to trial fit pretty much everything, and this is what I have so far... INPUT IS WELCOME AND ENCOURAGED!
The distributor and drive gear
Basically it looks like I need a spacer to take up the excessive end play. It must be closer to 3mm on both the old and new case using the stock dizzy. To make matters worse, I just found out that Volkspares sold me a dizzy which with a hopelessly long drive shaft. They machine it for the clamp, but it doesn't seat right and is impossible to set the end play properly
Plan is to machine a spacer on the lathe ( a good starter project), but don't know what to do with the dizzy. Will probably take it back and try to swap it out for something actually fits.
Thoughts on the spacer and a new distributor?
The cam gear
It looks like the cam gear I have is just slightly oversize. There is no backlash and although rotating the crank doesnt cause the cam to jump out completely, but I can hear and feel it hopping up just enough to make me concerned. There is no size marked on the gear (@Tony, got this from you a while back) so not sure what it should be. Should I be concerned enough to swap it? Can one fix this by running the gears together with a bit of fine lapping compound, like I read here:
http://haysvwrepair.com/rebuilding-an-a ... toy-style/ (roughly half way down on the installing the cam section)
The cooling fan
Also fitted the new Scat welded and balanced fan, but I found that when you use the stock spacers it rubs against the backing plate. So It needs a massive spacer to get the clearance needed which means there isn't a lot of thread left for the nut. I also doesn't run true and there is a lot of wobble. The stock fan fits fine, and has no visible wobble. Anyone had a similar experience with the depth of the fan, rubbing and wobble? I don't feel that it's a bent alternator shaft.
(Will try upload a video)